Freitag, Juli 04, 2008

...why did I loose my vertical foil?

Not a good Tuesday for sailing the Moth. Weather wise it was OK. The wind had shifted to the East. Nice and warm in the evening at around 19.00h when I hit the water. 10 - 13 kn. Everything went smooth with the set up and I felt ready to try again some foiling jibes. Not that I am managing this maneuver by now but after a bit of foiling high and dry the boat did not want to come up on the foils after a tack. Strange feeling. The bow deep in the pond. Me crawling to the back of the tramp but no change. The boat did not come up. Checking the ball joint, which connects the wand to the centerboard, it was OK. Back to shore. My worst thoughts had happened. The foil had disappeared. It took the thread of the stainless steel rod with it and pulled the M6 screw out of the carbon thread. Even today I have no idea how that could happen. There was no grounding and no feeling of hooking in to a net from the local fishermen. Just strange.

What made it really disappointing is the fact that on Sunday I had a really pleasant sail with this set of foils (the first ones, delivered with the boat. The ones which I had leant out till last week) and I thought that I should make notes about the set up, the angles etc. OK, I took a photo and marked the two sets. Now there is some work to do. Hope that our friends at Bladerider are able to supply spares soon. Another breakdown and I can skip the planned regatta activities.

Wednesday night race with the Bull (the little blue one on the pic.) was an interesting one. The thermal wind from the east made the windsurfers happy. In the "channel" we had about 5 Bft gusting a bit higher. With the "boys", Jan and Söhnke it felt OK. A little bit light on crew weight, therefore a reef and the small jib. A decent start because an early starter gave us some problems first. Lot´s of flogging mainsail around us. Most boats did not put a reef in. Even we got some big hits and nearly laid flat on the water but after a while got the hang of it. Got the boat going against the longer waterline boats. The X-34´s and the X-99 were gone when we came into the narrow navigable water. We had to fight more than usual as we nearly got stuck in the "crowd". With a draft of 1,70m against the 1,30m-1,40m going H-Boats and Folkboats we had to get it right. And we came out this narrow path as second boat from the tight bunch. We were than able to sail longer stretches, only two tacks on the laylines and got around the weather mark in fourth position. Henning with his X-79 had sailed clever and fast and was in front of us. We had a good ride with the gennaker and came close to the X-79 looking out for the wing mark. What we saw was ugly. No mark but the 99´and the 34´had entangled with each other and the buoy. They dragged it downwind. Henning and I decided, enough is enough and rounded an imaginary buoy and on to a tight reach. After that another beat into the wind and than the long downwind. Gennaker up and we made 11kn easy. In the gusts the speedo climbed up to 13kn. Should shake the reef out but we did not know what to expect in the "channel". Windsurfers were blasting forth and back. We came close to the X-34 and the crew hoisted their kite. Only to broach after it was set. We flew to the downwind mark, had a good round with our typical windward drop and were able to hold the first position into the finish. Abt. 2.45min in front of the X-79, our toughest competitor. It gave us a first place on corrected time and some confidence that we can do it with the Bull also in the heavy stuff. Thanks to my crew. The "boys" have learned a lot since we first sailed the Bull together ten years ago. Wishing them all the luck they need in the upcoming Int. 14 Skiff World Championship in Warnemünde next week.

3 days of sailing for my (not installed) sailing counter.

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